Production Facility
Assessment & Goal Setting
Following the installation of new packing facility Clarke Optimal were tasked with the energy saving drive within the existing building to enable the site to become a more efficient manufacturing operation.
Implement & Deliver
Assessment was conducted to ensure all assets were analysed and monitored.
Operational assessment was carried out to decide on essential and non-essential plant. Essential plant was optimised to maximise efficiency whilst maintaining the requirements for the environment. Redundant plant was decommissioned to realise maximum energy savings.
Achieve Goals & Analyse
Huge energy savings have been verified and realised from the assessment carried out.
Area A1 | Area A2 | Area B | Area C4 | |
---|---|---|---|---|
Co2 Savings (Tonnes) | 121.3 | 61.4 | 64.5 | 710.1 |
Grand Total Cost Savings | £80,637 | £33,636 | £52,923 | £377,029 |
Return On Investment (ROI) Months | 2.9 | 2.0 | 4.0 | 8.0 |
Achieve Goals & Analyse
Huge energy savings have been verified and realised from the assessment carried out.
Co2 Savings (Tonnes)
Area A1 121.3
Area A2 61.4
Area B 64.5
Area C4 710.1
Grand Total Cost Savings
Area A1 £80,637
Area A2 £33,636
Area B £52,923
Area C4 £377,029
Return On Investment (ROI) Months
Area A1 2.9
Area A2 2.0
Area B 4.0
Area C4 8.0
Pharma Production Facility 42% Reduction


Calculated Predicted Energy Savings
